by Admin | Feb 25, 2019 | Audi
This 2006 Audi A4 Avant had a slipping clutch before it stopped completely and the pedal fell to the floor. We could tell immediately by the clutch friction material fibers falling out of the bellhousing that the clutch had completely come apart. We proceeded to...
by Admin | Feb 19, 2019 | Volkswagen
This 2010 Tiguan came in for a misfire fault. It was determined that the fuel injectors were leaking which necessitates intake manifold removal. This was combined with a carbon cleaning procedure which uses a walnut abrasive blaster to remove carbon buildup from the...
by Admin | Feb 11, 2019 | Mini Cooper
This R56 Mini Cooper came in with a bad stumble on acceleration which we determined to be a faulty ignition coil. While diagnosing we removed a spark plug and found the plugs looked original at 65k miles. The manufacturer recommends spark plugs at 60k miles, but as...
by Admin | Feb 4, 2019 | Porsche
This 2005 Porsche Boxster S came in for routine maintenance, but upon further inspection, we found the accessory belt tensioner had disintegrated. Amazingly, this did not disturb the belt and it was running quietly on the bearing from the tensioner pulley....